Well, compression test says 150, 150, 0, 0.
I can hear the air rushing from 3 to 4 when testing 3, and 4 to 3 when testing 4.
Starting the teardown now. Waiting for the coolant to drain overnight, and will continue tomorrow after work.
Hope it's just the head gasket, but I'll find out more as things progress.

Thanks!


1986 Pickup extracab longbed "Woody edition"
SAS - 33's, 5.29's, lockright rear.

02 IS300 SportCross - my "DD"
94 2wd v6 extracab
04 Outback Wagon- wife's/family car