ok well I got him to come over and not buy the 22r decreased his motor again got it all dried off started it and let it idle and no leak the instant he gave it some gas oil started flinging off of the crank pulley shut it off and inspected the whole front of the motor no oil from the head.

so we looked a little closer at the crank pulley and oil was dripping so we pulled the radiator and fan to inspect the front main seal got everything out and he went to loosen the crank bolt and it was LOOSE since we where at this point we pulled the old main seal it was worn and old.
put in a new one I had laying around put the sucker back together torqued it to spec filled it all back up with fluids started it up and saved him a ton of $$$$$
no leaks now I am gald he listened to me and came over he was going to take the extra head I have over and get it
re done today but he waited

now we have to find out how a bolt that should be torqued at around 119 flbs loosened up after the exhaust was fixed witch we had to tighten some bolts on and had to change.


1989 toyota 4runner 5speed 4" lift